Sunday, September 13, 2015
Security Cameras are Pointless
Sometimes, having a security camera is pointless. Here is one of those times :
If you can't prevent the hurt from your eyes, how do they help? Thanks for the laughs, Jeff and Mike!
Monday, August 24, 2015
Bringing Compassion (Ashley Madison)
In June of 2015, a breach of security happened with a company called "Ashley Madison" - a purveyor of cheating spouses, secrets, and probably a lot of illicit behavior. Under request of someone I know, I obtained the data from that event, trying to run a little bit of profiling. The data (compressed) occupied over 10Gb. That is a lot of data. It expanded to about 20Gb. That is a ton of data. When I imported into a temporary database, it expanded to around 45Gb of data. Yes, 45Gb of damning, dark data.
Curiosity got the better of me and I wanted to do some statistics on it. So, I tried running a few numbers. In the process of running a few numbers, I accidentally forgot to pipe the data through the counting mechanism on a single command (I did not make that same mistake again), and it started dumping names to the screen. As I frantically smacked "CTRL-C" over and over and over in an attempt to cancel that, I was unfortunate enough to witness a few names scroll past. These were people that I knew. These were people that I had full respect for one week ago.
That happened two days ago.
I cannot get that out of my head. As much as I'd like to say that I am not judging, deep down I can just feel the results of their heavy falls from the pedestals on which I had placed them. The reverberations of simply knowing someone elses sin can lead to two reactions:
Now, what do you do when you know this? How do you react? The age old question, what would Jesus do? It brought to my mind the incident of the Savior, when the woman that was caught in adultery was brought to him. There were two teachings that came about when this occurred:
So, how should we be reacting? Do you want to be the first to cast stones? Or even the last? I grew up at dear old Davis High School. I hated high school. I was an outcast. I know what an outcast feels like. I have been there. I have experienced it.
Here are some numbers. In Kaysville, Utah (population of 28,000), there were 932 credit card transactions. Of those, there were 140 people caught up in that in the city. In Centerville, Utah (population 16,600), there were over 900 people caught in the data leak. In Bountiful, Utah (population 43,000), there were over 1200 people caught in that. That is well over 2 thousand people that many call neighbors, friends, or family that fell victim to the desires that should be kept between husband and wife. That is the fall of Helaman's 2000 stripling warriors.
As these people begin to pick up the pieces of their lives that have just crumbled to the ground in a big pile of crap, please take time to do a few things :
Curiosity got the better of me and I wanted to do some statistics on it. So, I tried running a few numbers. In the process of running a few numbers, I accidentally forgot to pipe the data through the counting mechanism on a single command (I did not make that same mistake again), and it started dumping names to the screen. As I frantically smacked "CTRL-C" over and over and over in an attempt to cancel that, I was unfortunate enough to witness a few names scroll past. These were people that I knew. These were people that I had full respect for one week ago.
That happened two days ago.
I cannot get that out of my head. As much as I'd like to say that I am not judging, deep down I can just feel the results of their heavy falls from the pedestals on which I had placed them. The reverberations of simply knowing someone elses sin can lead to two reactions:
- Throw stones at them (stones could be ridicule, insult, or even turning away from them)
- Give them a little room and allow them to try and pick up the pieces of their lives
Now, what do you do when you know this? How do you react? The age old question, what would Jesus do? It brought to my mind the incident of the Savior, when the woman that was caught in adultery was brought to him. There were two teachings that came about when this occurred:
- No one is without sin, so be careful about casting the first stone
- If you are the one caught in it, stop doing it.
So, how should we be reacting? Do you want to be the first to cast stones? Or even the last? I grew up at dear old Davis High School. I hated high school. I was an outcast. I know what an outcast feels like. I have been there. I have experienced it.
Here are some numbers. In Kaysville, Utah (population of 28,000), there were 932 credit card transactions. Of those, there were 140 people caught up in that in the city. In Centerville, Utah (population 16,600), there were over 900 people caught in the data leak. In Bountiful, Utah (population 43,000), there were over 1200 people caught in that. That is well over 2 thousand people that many call neighbors, friends, or family that fell victim to the desires that should be kept between husband and wife. That is the fall of Helaman's 2000 stripling warriors.
As these people begin to pick up the pieces of their lives that have just crumbled to the ground in a big pile of crap, please take time to do a few things :
- Give them a chance to change. The Savior did that very thing so many times.
- Remember that they are now fighting a battle that we have never even imagined. It is resulting in life-ending suicides, divorces (and future divorces), and shattering of everything they have ever known.
- Please bring compassion to the table. They are going to need as much compassion as they can get.
I am personally grateful that I know the Savior's atonement applies to everyone, including those caught in the Ashley Madison leak. We need to remember that at the judgement of God, our own "Ashley Madison" data leaks will occur. Even now, every bad thing we have done is already known. We cannot hide that fact. It all comes out in the end.
So be kind. They get to experience a little of that judgement earlier than we will. And we will experience it.
Labels:
ashley madison,
christ,
compassion,
god,
jesus,
judgement,
life,
repentence,
savior
Monday, August 17, 2015
3D Scanning - Proof of Concept
Just as a test, I grabbed the Skanect software, an adapter for the Kinect 360, and the sensor from our Xbox. I wanted to see if I could scan something in. The best thing I could think of quickly was the broken down tiller. It didn't turn out too bad!
https://drive.google.com/open?id=0B-DqTExptE5aRjBXTnZOUG1GaUE.
I also exported it and imported into Blender :
A try at embedding it in the page (might take a while to load, since it's 57.3M) :
Saturday, August 15, 2015
Lathe Compound Slide Refinished
I received the compound slide for the lathe yesterday, and promptly (of course, after mowing the lawn and spraying herbicide all over the lawn to try and kill the weeds) set to work cleaning it up and refinishing it.
The first thing to do was to take it apart. Yeah, you read that right.... I want to take it apart, and there are two reasons for that. First, I want to have every part cleaned - no old grease, no rust, no dirt, no old metal flakes in there. Second, I repainted the lathe, and it would be fairly nice if the tooling matched. So, off I go.
Surprisingly, it only took a few minutes to have it in pieces. I already knew the carriage (the bottom casting) for this lathe matched the right part number (L2-51). I didn't know if the rest of it matched up.
The swivel slide (the second cast iron piece) did match up as well (L2-52). It is separated from the carriage (L2-51) by way of the compound rest swivel (part 9-301):
I could not validate that casting as it was aluminum, and had no part number stamping. Riding on top of the assembly is the tool post slide, part number L2-53 :
While apart, I wanted to know if the tool post slide could be replaced with something that would allow me to use the lathe as a simple mill. It's a nice angled mechanism that keeps things in a solid state, so there is no reason why we can't :
Once I had it apart, I threw some acetone at the parts to clean the old paint off. This took the longest chunk of time. I had already picked up some self-etching primer from Sherman-Williams, so I masked off the surfaces that weren't painted with machine gray, and sprayed primer all over.
I used two coats of primer, and then sprayed three coats of Sherman-Williams blue. I had used the cap that was a close match to the original blue (the cap was slightly lighter in color, but you know, that "cap indicates color" thing means it should be close enough). Unfortunately, the final blue was more of a sky blue. Yeah, the cap color was half way between the original blue and the color of the sky. Still, it doesn't look too bad :
While at it, I dismantled the tool rest, the tailstock, and the headstock for the lathe, and cleaned up and painted them. The only thing left to refinish is the lathe bed. I can't test-fit the tools to the lathe bed, either, because I just don't have it right now - I had sent it off to a good ol' welder to braze a crack. But, as soon as it comes back, it will be time to take the labels off the bed, strip the paint off, and refinish that, too. Then I can put it back on, and find a milling attachment for the compound slide. Woohoo!
Saturday, August 8, 2015
Shop Footprint - Lathe Table Hack
I don't have a lot of room for a "shop". Actually, I do have room. It's about 5'x10'. That's not a lot of room for anything but storing tools, not actually using them. As a result, I'm all about trying to reduce my "shop" foot print.
One thing I've acquired is an old Craftsman wood lathe (becoming a wood/metal lathe). It came with a table under it that was fairly solidly built (half-square steel channel, welded together) - about 2'x4'. There is a problem with the table ... it's heavy. So much so that it is a bear to move to where I can use the lathe, and then put it away.
So, I opted for the next-best thing. I welded a steel square tube to the feet, drilled holes, and painted it. It allows me to throw caster wheels on when I need to move the thing around, and take them off when turning. Sometimes, I amaze myself (you should be thinking, "if that's all it takes, there are probably issues there).
While I was at it, I welded some angle iron to the frame, and riveted a chunk of peg-board up. That allows me to keep my tools with the lathe, without them being in the way. I also riveted a hinge (simply a "custom angle anchor") and another piece of peg board up, and had a sand-paper storage on the tool "rack".
On the other side of the peg board, I riveted a plastic storage container down to hold spare chucks, spindles, etc.
I also grabbed some 1/16" wire "rope" (cable), and connected a hammer, a wooden "mallet surface" (something I can hit with the hammer and not damage tooling), and a printer rod...
... wait, what?
Yeah, a printer rod. I took a printer rod, cut it down to size, and, since it had a hole in one side, I cabled it up to the lathe. It is a perfect size to slip inside the headstock spindle and is used to drive out the Morse Taper #1 (MT1) bits. Since it's cabled to the table, it's always available. Now my table is complete, mobile. The next task is to add some adapters to add a lead screw, making this a complete metal lathe with a compound slide. I already sold my AK47 - the funds are helping purchase a 3D printer! Can't wait!
One thing I've acquired is an old Craftsman wood lathe (becoming a wood/metal lathe). It came with a table under it that was fairly solidly built (half-square steel channel, welded together) - about 2'x4'. There is a problem with the table ... it's heavy. So much so that it is a bear to move to where I can use the lathe, and then put it away.
So, I opted for the next-best thing. I welded a steel square tube to the feet, drilled holes, and painted it. It allows me to throw caster wheels on when I need to move the thing around, and take them off when turning. Sometimes, I amaze myself (you should be thinking, "if that's all it takes, there are probably issues there).
While I was at it, I welded some angle iron to the frame, and riveted a chunk of peg-board up. That allows me to keep my tools with the lathe, without them being in the way. I also riveted a hinge (simply a "custom angle anchor") and another piece of peg board up, and had a sand-paper storage on the tool "rack".
On the other side of the peg board, I riveted a plastic storage container down to hold spare chucks, spindles, etc.
I also grabbed some 1/16" wire "rope" (cable), and connected a hammer, a wooden "mallet surface" (something I can hit with the hammer and not damage tooling), and a printer rod...
... wait, what?
Yeah, a printer rod. I took a printer rod, cut it down to size, and, since it had a hole in one side, I cabled it up to the lathe. It is a perfect size to slip inside the headstock spindle and is used to drive out the Morse Taper #1 (MT1) bits. Since it's cabled to the table, it's always available. Now my table is complete, mobile. The next task is to add some adapters to add a lead screw, making this a complete metal lathe with a compound slide. I already sold my AK47 - the funds are helping purchase a 3D printer! Can't wait!
Saturday, June 27, 2015
Original Lathe AC Motor Rebuilt
I broke the lathe. Yes, I broke it that fast. I was turning a pen for a neighbor, and plugged it in for some final sanding, there were some arcs and sparks (both in the motor and in the power cord end that I was holding), and it stopped working.
I started looking at DC motors. Here's what I needed - a motor with a 1/2" shaft, 1/3 Horsepower, and (preference here) direct current with variability in RPM. I finally gave up and decided to crack the original motor, trying to locate the start capacitor in case I could track a new one down. Don't get me wrong, there are motors out there, but they were all priced in the $300-$800 - and I wasn't plopping that kind of cash into the Ebay ecosystem.
So, I cracked it open.
I noticed a few things :
I found that there wasn't a start capacitor in this motor. It is actually a mechanical assembly.
I also realized that there were oiling channels for the motor bearings, on each end of the case. Thinking they were plugged with old saw dust, I grabbed the air nozzle again and tried to blow them out. Turns out they weren't plugged, but it's some sort of a sponge in there to keep the oil so it would channel into the bushings/brearings. There are grooves on the inside of the casing angled in such a way to put oils around the bearings. Quite ingenious, if you ask me.
After soldering a replacement power cord into place (and fixing a few other things while I was at it in the electrical system), I buttoned it all back up, and plugged it in... success! Proud to have a working original motor connected to the lathe still, costing $15 of repair (for the replacement power cord, which had gouges in it exposing the aluminum wire and making it a bit dangerous). I get my man card back again.
I started looking at DC motors. Here's what I needed - a motor with a 1/2" shaft, 1/3 Horsepower, and (preference here) direct current with variability in RPM. I finally gave up and decided to crack the original motor, trying to locate the start capacitor in case I could track a new one down. Don't get me wrong, there are motors out there, but they were all priced in the $300-$800 - and I wasn't plopping that kind of cash into the Ebay ecosystem.
Model: | Dunlap (Sears) model 15.4624 |
Volts: | 110 |
Speed: | 1750 RPM |
Horsepower: | 1/3 |
Amps: | 6 |
Shaft Size: | 0.5" (or 1/2") |
So, I cracked it open.
I noticed a few things :
- It had a switch (yeah, I didn't see that before because it was on the back side of the motor).
- I moved on and found where the wiring went into the casing had worn out, and the wires (made of aluminum) had been exposed to the metal casing - that would be an additional cause of the arcing and sparking.
- It was DIRTY! I grabbed the air compressor nozzle and cleaned it out quickly, but made a nice mess of the back patio in short order.
I found that there wasn't a start capacitor in this motor. It is actually a mechanical assembly.
I also realized that there were oiling channels for the motor bearings, on each end of the case. Thinking they were plugged with old saw dust, I grabbed the air nozzle again and tried to blow them out. Turns out they weren't plugged, but it's some sort of a sponge in there to keep the oil so it would channel into the bushings/brearings. There are grooves on the inside of the casing angled in such a way to put oils around the bearings. Quite ingenious, if you ask me.
After soldering a replacement power cord into place (and fixing a few other things while I was at it in the electrical system), I buttoned it all back up, and plugged it in... success! Proud to have a working original motor connected to the lathe still, costing $15 of repair (for the replacement power cord, which had gouges in it exposing the aluminum wire and making it a bit dangerous). I get my man card back again.
Thursday, June 4, 2015
Newest Tool (#534.0601 Dunlap Wood Lathe) (Wish It Were a Kid Instead)
I just have to welcome the newest member of the shedhold (not household). I managed to locate an old Sears/Craftsman/Dunlap wood lathe (model #534.0601) for a fairly good price. The tailstock didn't line up with the headstock (later found it was adjustable, see below). I wouldn't have budged on this one, except the manual (located on the vintage machinery site main article and also a direct PDF link) had this little blurb in it reading :
Oiling
Adjusting the Tailstock
Removing Tooling
Obtaining Parts
Summary
So I bit down and picked it up. I grabbed some stamped/cast part numbers, found the manual out there, and pulled as much info as I could. Here are some numbers I've been able to locate so far:
It appears to be in great shape for it's age (around 1942). It runs (well, ran, the motor just gave up the ghost - and I had to rebuild the motor to get it working again). Here are some quick photos.
When I cracked the top cover open, I found it had an indexed pulley in the headstock.
It's broken into 60 indexing holes, and has an indexing pin to stop the pulley from spinning. The manual listed the following indexing table :
The manual also lists turning speeds (for wood) :
It rotates freely, the motor actually fired up for a while (it's the original motor, Dunlap 115V model #115.4624 1/3 HP with a 1/2" drive shaft), then it stopped working (arcing and sparking) and was then rebuilt, and seems to function fairly well.
The previous owners had also left some bits in the headstock and tailstock. I was initially glad they did, thinking it would have prevented corrosion from getting into the taper mounts. When I started looking at how to remove the tooling, I soon realized that the spindle is hollow, and that meant my initial thinking was invalid - corrosion could get to the inside of the main spindle. The tailstock was in great shape.
First step - oil it!
I threw some oil into the tailstock, in the following way. I adjusted the ram (the thing the live center or chucks press into) all the way out, and it slid right on out. I throw some oil on it, and worked it into the tailstock and out of it completely numerous times. Then, while I had it out, I threw some oil into the back end (where the handle connects to the ram), and worked that a few times. If it had a bolt, I removed it and oiled it. It got to a point that it was working fairly nicely.
Next, I pulled off the tool rest and dismantled it. I did not remove any "rust" (it looked like dust, and I didn't want to lose any metal), so I simply added some oil to everything and put it back together, then took it apart again repeatedly, oiling between each assembly to ensure I had it everywhere. Again, I cleaned up threads on the hold-bolts, then oiled it once more and assembled.
I filled the oil cups on the headstock, and put on some turns by hand, just because I needed to ensure the front oil cups are working, and not sealed with gunk before I fire it up for any real use. I grabbed an oil rag and wiped the headstock down, squirted some oil against the spindle bushings while turning it and sliding it back and forth in the headstock just to get some oil penetration.
Once I vetted that the level of oil in the cups had dropped, I filled the cups again and fired it up. I ran it for a few seconds before it stopped turning, and I simply started to go crazy and shut it off.
Then I realized the spindle had a wheel on it that was too tight. I loosened that, and fired it back up. Success!
Second step - see about the misaligned tailstock!
So, I started poking around the tailstock to see about the misalignment :
I found at the bottom what looked like threaded rod with a slot cut into it (circled in red) :
Pulling off the tailstock from the ways, I found that they were completely separate rods, not a single one :
I realized that they are two separate rods, one on each side, and they will push against an alignment block on the tailstock. Yes, that is the tailstock base part number cast, L2-6A. I greased up the threaded rods to get them to turn, cleaned them out, reassembled, and promptly had the tailstock lined up with the headstock. Just as an FYI, here's the tailstock housing part number stamp :
Removing the Tooling :
The tooling is removed like this. Because the spindle is hollow (I might have to turn a solid spindle to be used in metal work just to make sure it will hold the pressures), you need a long rod (not threaded - you don't to mar the inside of the spindle). Insert this from the back end of the spindle by hand until it travels over half way through the spindle and makes contact with the end of the tooling. Grab your hammer, and give it a light tap or two, until the tooling pops loose.
The tailstock tooling is a bit (that's still not very punny) easier to deal with. Initially, I thought the tailstock ram simply did not move all the way into the tailstock - I still had about 3/8" left of ram when it "bottomed out". After watching one youtube video that was using a modern lathe (who still makes a lathe with the hard-to-find #1 Morse Taper/MT1 bits?), I had the thought that it might be bottoming out on the back side of the tooling. I retracted the ram until it bottomed out, then put some cranking onto the hand wheel, and it popped right out. Here's the tailstock photo, in which you can see how far the ram was retracting before we popped the tooling out :
After popping out the tooling, I could do a little more cleaning. I found a crack, and I had to have it welded, and then I needed to check it for straightness (flatness) on the bed ways for warping.
Third - Obtain Parts
At this point, I have a fully operational lathe that I can't use. Yes, it works, but not very well, since the headstock only has an MT1 center spur shank in it, and the tailstock has a dead center cup (dead, meaning it isn't supposed to turn). I can't put any stock between (because the tailstock doesn't spin), so I'm stuck until I track down some parts. Here's what I'd like (order of importance because of usefulness) :
Summary
This is a fairly nice lathe, considering it's age (73 years). It's real cast iron, not the new white metal (pot metal/zinc alloy), fairly rigid, and has been used to turn a pen already, and has done the roughing on a second pen, as well as cut down a 2"x4" chunk of wood for a taper setting tool. It's been a great introduction to the lathe tools, and will provide a great base for increasing capabilities!
"This lathe can be made into a metal turning lathe by equipping it with the compound tool rest...
"... Important: Use only the slowest speed and take light cuts. (These slower speeds can be obtained by our Jackshaft, see Cat.)"That means to me the bed is rigid enough to work for what I need.
Oiling
Adjusting the Tailstock
Removing Tooling
Obtaining Parts
Summary
So I bit down and picked it up. I grabbed some stamped/cast part numbers, found the manual out there, and pulled as much info as I could. Here are some numbers I've been able to locate so far:
Bed Gap: | 1 3/4" |
Motor: | Original Dunlap 1750 RPM, 1/3 HP, Model 115.4624, 1/2" shaft |
Turning Speeds: | 714, 1305, 2287, and 3952 RPM (smallest gear on motor pulley gives slowest speed) |
Headstock Spindle: | 3/4", 16 TPI (threads per inch), or internal Morse Taper #1 |
Tailstock Spindle: | Morse Taper #1 |
Part Number for Tool Post Clamp: | L2-18 |
Part number for Tailstock Housing: | L2-5A |
Part number for Tailstock Clamp: | L2-7 |
Part number for Tailstock Base: | L2-6A |
Compound Tool Rest Parts | |
Clamp: | L2-18 |
Carriage: | L2-51 |
Compound Rest Swivel: | 9-301 |
Upper Swivel Slide: | L2-52 |
Tool Post Slide: | L2-53 |
It appears to be in great shape for it's age (around 1942). It runs (well, ran, the motor just gave up the ghost - and I had to rebuild the motor to get it working again). Here are some quick photos.
When I cracked the top cover open, I found it had an indexed pulley in the headstock.
It's broken into 60 indexing holes, and has an indexing pin to stop the pulley from spinning. The manual listed the following indexing table :
Divisions Desired | 1 | 2 | 3 | 4 | 5 | 6 | 10 | 12 | 15 | 20 | 30 | 60 |
---|---|---|---|---|---|---|---|---|---|---|---|---|
# of spaces | 60 | 30 | 20 | 15 | 12 | 10 | 6 | 5 | 4 | 3 | 2 | 1 |
Degrees of Arc | 360 | 180 | 120 | 90 | 72 | 60 | 36 | 30 | 24 | 18 | 12 | 6 |
The manual also lists turning speeds (for wood) :
Size Diameter of work | Roughing Cuts | General Finish Cuts | Fine Finish Cuts - Sanding |
---|---|---|---|
Up to 2" | 2,297 | 3,952 | 3,952 |
2" to 3" | 1,305 | 1,305 | 2,297 |
3" to 4" | 714 | 1,305 | 2,297 |
4" to 5" | 714 | 1,305 | 1,305 |
5" to 6" | 714 | 714 | 1,305 |
6" to 7" | 714 | 714 | 1,305 |
7" to 10" | 714 | 714 | 714 |
It rotates freely, the motor actually fired up for a while (it's the original motor, Dunlap 115V model #115.4624 1/3 HP with a 1/2" drive shaft), then it stopped working (arcing and sparking) and was then rebuilt, and seems to function fairly well.
First step - oil it!
I threw some oil into the tailstock, in the following way. I adjusted the ram (the thing the live center or chucks press into) all the way out, and it slid right on out. I throw some oil on it, and worked it into the tailstock and out of it completely numerous times. Then, while I had it out, I threw some oil into the back end (where the handle connects to the ram), and worked that a few times. If it had a bolt, I removed it and oiled it. It got to a point that it was working fairly nicely.
Next, I pulled off the tool rest and dismantled it. I did not remove any "rust" (it looked like dust, and I didn't want to lose any metal), so I simply added some oil to everything and put it back together, then took it apart again repeatedly, oiling between each assembly to ensure I had it everywhere. Again, I cleaned up threads on the hold-bolts, then oiled it once more and assembled.
I filled the oil cups on the headstock, and put on some turns by hand, just because I needed to ensure the front oil cups are working, and not sealed with gunk before I fire it up for any real use. I grabbed an oil rag and wiped the headstock down, squirted some oil against the spindle bushings while turning it and sliding it back and forth in the headstock just to get some oil penetration.
Once I vetted that the level of oil in the cups had dropped, I filled the cups again and fired it up. I ran it for a few seconds before it stopped turning, and I simply started to go crazy and shut it off.
Then I realized the spindle had a wheel on it that was too tight. I loosened that, and fired it back up. Success!
Second step - see about the misaligned tailstock!
So, I started poking around the tailstock to see about the misalignment :
Tailstock toward the bottom of the picture, headstock to the top, from above the lathe - quite a difference |
I found at the bottom what looked like threaded rod with a slot cut into it (circled in red) :
Pulling off the tailstock from the ways, I found that they were completely separate rods, not a single one :
I realized that they are two separate rods, one on each side, and they will push against an alignment block on the tailstock. Yes, that is the tailstock base part number cast, L2-6A. I greased up the threaded rods to get them to turn, cleaned them out, reassembled, and promptly had the tailstock lined up with the headstock. Just as an FYI, here's the tailstock housing part number stamp :
Removing the Tooling :
The tooling is removed like this. Because the spindle is hollow (I might have to turn a solid spindle to be used in metal work just to make sure it will hold the pressures), you need a long rod (not threaded - you don't to mar the inside of the spindle). Insert this from the back end of the spindle by hand until it travels over half way through the spindle and makes contact with the end of the tooling. Grab your hammer, and give it a light tap or two, until the tooling pops loose.
The tailstock tooling is a bit (that's still not very punny) easier to deal with. Initially, I thought the tailstock ram simply did not move all the way into the tailstock - I still had about 3/8" left of ram when it "bottomed out". After watching one youtube video that was using a modern lathe (who still makes a lathe with the hard-to-find #1 Morse Taper/MT1 bits?), I had the thought that it might be bottoming out on the back side of the tooling. I retracted the ram until it bottomed out, then put some cranking onto the hand wheel, and it popped right out. Here's the tailstock photo, in which you can see how far the ram was retracting before we popped the tooling out :
Tooling installed, you can see the ram with two different styles, one wet with oil, the other dry. This is the line where it would stop on the tooling. |
After popping out the tooling, I could do a little more cleaning. I found a crack, and I had to have it welded, and then I needed to check it for straightness (flatness) on the bed ways for warping.
Third - Obtain Parts
At this point, I have a fully operational lathe that I can't use. Yes, it works, but not very well, since the headstock only has an MT1 center spur shank in it, and the tailstock has a dead center cup (dead, meaning it isn't supposed to turn). I can't put any stock between (because the tailstock doesn't spin), so I'm stuck until I track down some parts. Here's what I'd like (order of importance because of usefulness) :
Live Center for the tailstock- this would allow me to turn something on this thing. I bought one.- Chuck for the headstock - this would allow me to throw a pen mandrel on this and start turning pens. I don't want an MT1 (or Morse Taper #1) chuck, I want a 3/4" 16 TPI 4 jaw chuck and backplate. It should be a machinist chuck, as the morse taper chuck is a separate item on my list. It COULD be a 1"-10TPI chuck with an adapter. I'll see what I can find.
Live Chuck for the tailstock- This would prevent me from putting too much stress on a pen mandrel. Speaking with a machinist in the neighborhood, I was instructed that this would be pointless - he never uses one - and that a good live center would be better. So, I scratched this one off my list.Dead Chuck (MT1, or Morse Taper #1) for the tailstock- something to put a drill bit in (yes, the bit won't turn) so that the work will turn around the bit, ensuring a perfectly centered hole. This can also be jammed into the headstock for the pen turning. I couldn't find one, so I bought a morse taper arbor and a matching chuck, assembled them, and viola, I have one now.Compound Slide and Tool Post- I ultimately want to do some machining. To do this, I need parts L2-51, L2-52, L2-53, and another L2-18. If anyone has these parts lying around, please let me know. Well, I just barely found one listed on eBay. I know it's rare, so when I actually saw it, I quickly took that plunge.- A variable speed DC motor - that AC motor has got to go, sure, it works well, but it doesn't have enough torque for what I want to eventually do with it. Note, this might have to be bumped up in priority - the original AC motor gave out during a pen turning test. I did rebuild the motor because I wasn't ready to spend $300-$800 on a replacement, so it's not a requirement, because it is running. Before I start using it to machine metal, I need this - to turn the speed WAY down. The lowest speed on the lathe is 714 RPM, and that's way too high for machining metal.
- An RPM indicator - to get really effective, if you have a variable speed motor, this is the only sure way to know how fast you are spinning. Lots of DIY stuff around here, I might try this route.
A face plate- if I ever turn bowls, I'd need one. I probably won't turn any bowls, but the lathe originally came with one, so I ought to pick one up. I found a cheap one online, and installed it, but then took it off and haven't used it since.
Summary
This is a fairly nice lathe, considering it's age (73 years). It's real cast iron, not the new white metal (pot metal/zinc alloy), fairly rigid, and has been used to turn a pen already, and has done the roughing on a second pen, as well as cut down a 2"x4" chunk of wood for a taper setting tool. It's been a great introduction to the lathe tools, and will provide a great base for increasing capabilities!
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